Bullbar Swap

I was supposed to go camping over the long weekend just gone, but the weather turned bad (some epic storms last Friday) which turned everyone off camping.

On Saturday I ended up giving Rob a hand stripping the G60 that been sitting in his shed for the last few years. Mainly so that we could get Oscar into the shed for repairs so that Rob can come camping next time.

He wanted the doors, seats, steering box and the engine from this G60. The engine proved trickier than expected but because he doesn’t care about the chassis and body, the grinder got a decent workout, which made things easier. We won in the end.

On Monday I decided I needed to make some more headway on Snuffy, so dad and I set about swapping the bullbar over.

A shot of Skippy before we started:

I have hated the plastic bar that he came with since I bought it, it looks much better with the 3” lift (the bar looked outright wimpy before that) so it was good to finally see my good TJM bar go on. 

Because Skippy is a Series 3 and Snuffy a Series 1 there are a few differences that initially prohibited the bar from gong on, we had to cut a little bit out of the radiator guard (for some stupid reason the Series 3’s have a radiator that hangs down below the chassis, literally the only thing on the whole car that does). The grill also sticks out a bit more so we had to trim a bit out of the top of the bar as well. But it was worth it!

Now to find time to get the rear bar swapped...

My Final 2.8 Patrol Club Post

​Below is a copy of the last post I put into the 2.8 Patrol Club that I started in Facebook. Posted July 11, 2018

Its a sad time for me my friends, my beloved RD has died 😪

RIP Snuffy.

Somehow she got majorly dusted, I’ve been over the intake with a fine tooth comb and I can’t work out how it happened. The bores were badly damaged, even the big ends had grit go through them, every single one was nearly stuffed, and to top it all off the head was cracked, no symptoms from that yet but they cant have been far away.

I've just finished bolting 4.88 diffs gear in and a VNT Turbo onto her as well, never got to drive it! 😭

All of this is even more infuriating because I did a ground up rebuild in 2010, nothing was untouched! She's only done 95,000km since then!

Its taken me a while to digest everything that’s happened, but I have decided to buy a new vehicle (still a patrol) instead of dropping more $$ onto this one.

I started this club quite a few years ago now, it’s been great watching it grow and fill with people who like the RD as much as I do! Unfortunately my days of owing an RD28 are drawing to a close, but I’m not going anywhere, I'll hang around and continue to admin and contribute where I can.

Thank you to everyone for making the club what it is! I look forward to watching the mighty RD live on!

Snuffy Update

In short, Snuffy is buggered. RIP.

It turns out that Snuffy has suffered significant engine damage, we are unsure how it happened, but all indications are that it has been dusted, not only are the rings and bores stuffed, but the crank bearings appear as though they have done 600,000km, despite only having done just shy of 100,000km. This implies some crap (dust) has made it into the oil and gone through the engine.

So now I am looking down the barrel of a full ground up rebuild, like what I did in 2010.

Its frustrating being here again, we did all of this in 2010 after I stupidly left the sump bung loose. When we built it then we did everything properly thinking it would last me far longer than I would likely keep the car. Apparently not.

Snuffy

Well Shit.

Its taken me nearly a week to sit down and write this, and that’s because I needed to calm down, everytime I sat down to write something, anger over came me and I had to put it away.

Let me start at the beginning. Approx six months ago my car, Snuffy the Patrol, started blowing butt loads of smoke, oil smoke, the original turbo had crapped itself only 30,000km earlier and I had only been able to afford a secondhand unit in unknown condition from a wrecker on the mainland. Of course, I instantly assumed that unit had also crapped itself and so we went hunting for a replacement, I dearly wanted to fit an upgraded unit, maybe a Mamba kit or similar, but at about this time a low km (10,000km) set of 4.88 ratio diffs with ARB lockers came up for sale locally really cheap, I paid about $2000 plus my diffs, for perspective its nearly $5000 in parts alone! Its an upgrade I have long wanted to do, as it will return the gearing to standard with my 33" tyres on. So we bought the diffs, and opted for an aftermarket turbo.

Mistake number one.

The aftermarket turbo barely lasted a day, the test drive went really well, but on the first trip to work it started smoking again, the unit came with a 24 month warranty, which we attempted to claim on, but as it turns out upon a close reading its not worth the paper it is written on. So there goes $700 down the drain. Not to mention all the stress and headaches that went along with it.

That scared us away from aftermarket turbos, including Mamba kits and the like, so I went on the hunt for the best replacement, I didn’t want a genuine replacement as they just arent good enough for the engine, and also cost a ton to replace because they are a ‘s’ model, meaning Garrett built them specialy for Nissan for the RD28. Long story short I got onto a turbo specialist in Melbourne who was able to supply me a modified VNT Garret GT2056, which we jumped at, both dad and I have long thought that the RD needed a VNT, so despite the high cost we ordered one, knowing that a Garrett would last and not give us any trouble.

Fitting it turned out to be far more difficult that we were expecting, the supplied manifold adapter didn’t fit, the seller had made these units for other RD28’s and so had built mine to the specs he had in his records, even he couldnt understand why it didnt fit and offered a refund and his apologies. I was determined to make it fit and so we had Spreyton Engineering make up a new adapter.

In hindsight, mistake number two.

During all of this our Mini also had some issues, though these have been a long time coming and were only delayed due to lack of funds. Funds became available and after a series of, what we considered at the time to be very annoying events, but that I am now sure had the hand of God behind them, we found a new mechanic who was able to do the work, and I soon discovered, was very very good at their job. I have never been so impressed with a mechanic, and I have NEVER found any mechanic I was completely comfortable to leave my cars with. The best part is they are in Shearwater. Praise God.

I asked them to finish the turbo install on Snuffy for us because it was simply outside of our ability. I was blown away by the work they have done, the care taken, and the extra effort they went to.

That leads us to today, on Wednesday this week just gone they started Snuffy up for the first time since December of last year (2017), and that’s when the shit hit the fan.

It turns out that the turbo was never the problem. The problem is actually far more serious, the piston rings are stuffed. Why, I have no idea, its only done 100,000km, its been well looked after, regularly serviced, I’ve done everything right, but here we are. The only thing we can put it down too is a dodgy rebuild. We will of course know more once they get it apart, but you understand why I am so angry.

Basically whats happening is compression is making it past the pistons and into the crankcase, causing it to pressurize, because a turbo essentially relies on gravity to drain the oil from the bearings, if the crankcase is pressurized, the oil cannot drain, and so it gets forced past the seals and into the intake/exhaust, causing the engine to burn it. The reason the aftermarket turbo lasted a short while is because it took time for the crank to pressurize and also for the oil to make it through the intake plumbing, intercooler etc and into the combustion chamber.

This whole debacle has made me very angry, and it has taken time to calm me down. I just have to remember, at the end of the day it is just a car, and all its going to take to fix it is money, its just really really disheartening to put your very best into looking after something, and have it fail on you. I guess its just a fresh reminder of how broken the world is, and how much it needs Jesus.

Everyone, There's Someone I'd Like You to Meet

As most of you would know I have two cars, Snuffy the Patrol, and Leroy the Turbo Diesel Pug, a cheap to run runabout for daily commuting. 

When Amy and I got married we added Amys car, a Nissan Micra, known as Stevie, to the garage, giving us a grand total of 3 cars.. 3 cars for two people.. 

When we got married the Patrol was down an alternator and so having three was actually useful, but overall in the long run 3 is overkill and doesn't make much sense. 
Now the obvious solution here is to sell one and keep the other, right? Well, Yes, but that's boring. Amy has always wanted a Mini, and we had an opportunity to sell the Micra back to her parents, to become her sisters first car, and someone else is interested in Leroy, so we thought lets sell them both and see if we can find a Mini, so we went looking around..
Meet Sheldon: The John Cooper Works Mini Cooper

Amy has always wanted a Mini, and I have always liked the new models but never really considered owning one until now, I was happy to get Amy her dream car, but I thought, lets try and find a Cooper S, something I can have fun in too! So we went looking, we drove a clapped out Cooper S here in devonport, and we drove a boring run of the mill Mini in Evandale, and then I found Sheldon on gumtree, and it looked so good that I thought I just have to go and have a look at that, at the time I hadn’t considered it an option due to its price, I just wanted to have a look at the creme de la creme of Mini’s, and hopefully have a drive of it! 
 
Well I did, and I walked away thinking that would be the perfect Mini for us, only 2 owners, low kms, and has been extremely well looked after, the thing was spotless, and drove like a brand new car, even smelled like one! Despite being a 2008 model, so we bought it, and we love it, its fast, comfortable, and lots of fun! I find myself actually enjoying the trip now, not just keen to arrive at my destination. I enjoyed the Pug, but it was just a commuter car.
 
And the best part, it sounds amazing! It has a full stainless steel low back pressure exhaust system, it sounds great, and its loud enough to be noticed, but not loud like tho wankerish commodore etc getting about.
 
Here’s a link to a video I found on youtube showing what it sounds like, it sounds way better in person, but you’ll get the idea: https://youtu.be/XdoCJ0j0A4Y?t=599